VW

Or Maybe Not?

Tool Bag

I made some more progress with the bus today, but it also decided to stop working… again…

I started the day with another exciting shopping trip.  I purchased a sweet tool bag that will keep all the of the tools that I have had the pleasure of working with organized and mobile.  The plan is to keep this bag in the bus so I have access to just about anything I might need to fix problems on the road – this is part of the reason we bought this thing – it is so simple!  Basically three sizes of wrenches (13mm and 10mm and the big 21mm to turn the generator pulley), a flat blade screwdriver, and a few other odds and ends will allow me to do just about everything.  I’ve also included some carb cleaner, gloves, and some electrical stuff.  It feels good to get more organized, and setting this bag up is definitely a step towards a mobile camping bus!

I also test drove the bus some more – it started up great, ran beautifully, and everything seemed to be working out great.  I did notice that after the engine had been fully warmed, and running for maybe 15 minutes, the idle was fairly slow, and the exhaust was spitting out perfectly formed white smoke rings.  While this was kind of amusing, white smoke it not really a good sign.  I think its better than blue smoke (oil burning), or black smoke (gas burning), its still not good.

Then, at the end of the day, I decided to take one more trip around the lot – “you shouldn’t a dun that!” Backed the bus out, shifted to first fine, shifted to second – immediately lost power, and the engine died.  It wouldn’t start, but since I had my new onboard tool bag, I grabbed the carb spray and shot some of that into the carb’s fuel bowl. Engine starts, but dies almost immediately – I can’t keep it running!  I have to push the thing back to the garage, and then, with the help of my new bus friend Dennis, we got it pushed back into its home – what a fail!  I’m not really sure what happened, but it won’t stay running, idle speed wanders which is a sign of the dreaded air leak.  I bought a compression tester a while back, but never used it – I’m going to test each of the four cylinders – this should give me a rough sense of the engine’s health.  Its possible that now that I got it running for more than a few minutes, something inside the engine is worn out(valve rings, head seals, main seals, other things that I don’t even know about yet).  If the test is bad, I might be pushing up the date for a new engine!  In the mean time, enjoy this exciting and poorly done video of exhaust smoke rings:

Uncategorized, VW

Finally… Success!

Front Bus

As of today the bus runs beautifully!  I can start it, warm it up, drive it around, park it, and start it back up again.  While I’m still not 100% convinced that the engine is bullet-proof, it ran better today that it ever has before.

Switch Idle Jets

I started by swapping the power jet and idle jets.  Last week, I noticed that I reeked of exhaust fumes (more than usual) after working on the bus.  This is a sign that the carb is running rich – research suggested that these new 30Pict carbs come jetted incorrectly.  Sure enough, I noticed that the thing has two removable jets on the left side – idle and power jets, and one was slightly bigger than the other – I switched them around.

I also got some white paint and marked 30 degrees on the crank pulley – got out the timing gun, and revved the engine.  If it was timed correctly to 30degrees, the white paint should line up with the middle of the crankcase – however, when I revved that bad boy, the paint line was way off.  I twisted the distributor until the line shifted to the center – almost immediately, the engine idle smoothed out – Success!

Side Bus

 

Rear Bus

To cap off a very successful day, I drove Noelle around the parking lot a few times.  It started up with a bump of the key, and shifted gears beautifully.  I did manage to stall it once (because I can be an idiot, but that should be obvious by now) but it started right up afterwards so I could keep going. Basically, she thinks I am awesome and well I can’t really argue with that – I am very happy with the state of the engine now – I just hope the bus is still in a good mood tomorrow!

Uncategorized, VW

Another Week, Another Post

Manifold Parts

I was able to get a little more work done this weekend in between bursts of rain and wind. I left the bus last weekend with an ill-fitting carburetor, and a starter that sounded like it had died.  I tried starting it up mid-week, and noticed that it wouldn’t run at all, and after a couple turns of the key, the starter stopped turning over.  I also noticed a slight burning smell coming from the ignition with – not good!! Thankfully, I had just bought a bunch of VW parts from a local craigslist add – they ended up being all ’60’s Beetle parts, but the ignition switch is ’67 and might just work for the bus!

New Ignition Switch

However, when I went to start the bus today, I didn’t have any issues.  In fact, the thing starts with the slightest bump of the key, and runs beautifully!  I guess the bus is in a good mood today!  I ended up not replacing the ignition switch, but I’ve got it if I need it.  Instead, I pulled the carb and manifold off the engine… again… to try and fit the thing on there so that it isn’t leaking air.  I’m getting pretty good at this by now, but its still a big pain. Ok, manifold filed down flat (I still think its crazy that it came so jacked up), carb bolted on tight, everything put back together.

Burnt Carb Wire

I also noticed that the choke wire leading to the carb was burnt crispy – not good!  I replaced the wire, and will check it frequently to see if it happens again – I’m thinking its connected to my ignition switch issues.

Start the bus, it runs… but its still just not that great.  I still have some kind of air leak at the base of the carb – I spray the carb cleaner, and the engine changes speed.  It idles slow and gets rougher as the engine warms.  It lasts longer than the old carb/manifold, but after about 10 minutes or so, the engine finally dies if left to idle.  Once it dies, it is impossible to start.  I’ve heard about this problem – some call it heatsoak. Basically, everything heats up to the point where either the electrical connectors aren’t working, or the engine is vapor-locked.  I also think somehow that the engine could be flooding. So I suppose this is progress, its improved to a point where I could drive it around for a while, so I’ll be taking it out for some more parking lot circles in just a bit!

VW

More Carb Crap

New Carb Engine

My new 30pict carb and intake manifold arrived in time for me to get some serious work done this weekend.  What follows is a brief account of how I struggled to get this stupid bus engine working again – the end result – yeah it works… kind of.

I started Friday by pulling off the old carb and intake manifold.  I had done this before, but for some reason I really couldn’t get the pieces off the engine.  With a lot of effort, I was finally able to rip the old pieces off – the new manifold has detachable heat riser tubes that will make this job so much easier in the future!  I grab the new carb and decide to test fit it to the new manifold before I bolt everything on.  Thats when I notice that the two threaded studs that were included with the carb kit don’t fit into the base adapter plate.  They are just a little to big.  I pretty much freak out – WTF!  I have been very apprehensive that this new carb will be a piece of junk, and it looks like my fears are being realized.  I try to keep calm though – call the local Ace hardware store to see if they have different studs.  I take the new carb to the store, and the guy at the counter is an old VW nut from the ’70’s… Sweet!  He takes a look at the base of the carb, and pulls out a re-tapping kit – quickly twists an 8mm tap into the base holes, enlarging them enough to hold the threaded studs, solving my issues!

Back at home, I bolt the carb onto the new manifold – and notice my next issue.  The throttle assembly that links to the accelerator pump is rubbing on the base of the manifold – basically, the stupid thing doesn’t fit right!  Again I freak out – I’m ready to call the shop I bought this stuff from, and see what they can do.  Before I give up though, I decide to try and modify the manifold and throttle arm.  I bent the metal linkage ever so slightly to just clear the side of the manifold, and trimmed the new gasket – success!

By now its Saturday afternoon – I haven’t taken many pictures because I’m been to focused on getting this stupid thing to work!  Bolt that carb on, reinstall all of the cables and connectors when I notice problem #3 – the electrical connector on the carb is too big for the current connectors on the wires coming from the coil – off to NAPA to get new connectors!  Ok, that problem solved – the last step is to reattached the accelerator cable coming from the gas pedal… but it can’t reach the place where it attaches – WTF! this is problem #4 and its a big one.  I can force the cable to connect to the throttle piece on the carb, but it is stretching, and won’t let the gas pedal all the way up – not good!  I don’t know what to do – I’ve spent two days trying to get this stuff to work, and I have totally failed!

Fast forward to Sunday morning – I removed the adapter plate on the base of the carb (the same one I had to have re-tapped).  This lowered the base of the throttle, giving me just enough space to attach the accel cable – Success!  Until I tried to pull the throttle arm back – now problem #5 – the the carb is lower on the manifold, it catches on the side – oh, and I can’t fully bolt the carb down because there isn’t enough clearance for the two nuts – basically, the manifold is very poorly designed, and just doesn’t work well with the size of carb that I have (remember I’ve downsized from 34Pict to 30Pict…  I’m tired of dealing with this, so I do what I do best – try to destroy everything!  I bought a metal file from NAPA and went to town.  I was able to whittle the manifold sides down just enough to allow enough clearance for the throttle arm – Success!  I can now freely apply full gas pedal, and have everything close up properly on release.

New Carb Engine Running

Turn the key, pump the gas – it fires up!  The engine sounds beautiful, and it idles extremely well – even when full warm!  My problems aren’t completely over – it struggles to start, which might be a result of timing, or maybe I’m flooding the carb?, and I think I still have a small air leak at the base of the new carb – and the starter seems to be making some weird noises.  I’m sure I will address all of these issues soon, but in the mean time, I have a working engine again!  It took three days, and a ton of stressful one-off workarounds, but I’ve got this thing running again.  Yay!

Uncategorized, VW

Still Doesn’t Work!

Bocar Carb

Quick update on my carb progress – I haven’t made any!

I pulled my problematic 34pict 3 carb off the intake manifold again this week.  I’ve noticed a large air leak through the throttle plate bolt, and I tried to fix it.  It didn’t work – I pulled all of the jets and adjustment screws out, flushed everything I could with carb spray and compressed air.  I tried to tighten the bolts around the throttle plate, and sprayed the crap out of it to see if that helped.  Bolted it back on the engine – fired right up, ran beautifully…until it didn’t anymore. The engine starts to idle rough, and will eventually die as it warms up.  I can keep it running if I spray the carb cleaning fluid at the throttle bolts, or the blocked off intake ports.  Its all junk!

Carb Jets

I feel like I have given this carb my best efforts, and Noelle is ready for me to finally get this bus on the road – i bought a new stock intake manifold and a replacement 30pict carb from a shop in Cali.  I went with the older style 30pict instead of the 34pict based on some internets research, and the advice of the dude who sold it to me.  I don’t want to assume everything will just work when I get it all put together… but that would be awesome – the stuff shipped today, so I’m hoping my next post is all good news!